›› 2013, Vol. 34 ›› Issue (6): 1-1.

• 论文 •    

阿曼D油田水平井整体注水开发的实践

杨 双1,郭 睿1,赵国良1,黄 嵩2   

  1. (1.中国石油 勘探开发研究院,北京 100083;2.中国石油 新疆油田分公司 重油开发公司,新疆 克拉玛依 834000)
  • 出版日期:2019-01-01 发布日期:1905-07-14

Practice of Overall Horizontal Well Waterflooding Development of Carbonate Reservoir in OmanD Oilfield

YANG Shuang1, GUO Rui1, ZHAO Guoliang1, HUANG Song2   

  1. (1.Research Institute of Petroleum Exploration & Development, PetroChina, Beijing 100083, China; 2.Heavy Oil Development Company,Xinjiang Oilfield Company, PetroChina, Karamay, Xinjiang 834000, China)
  • Online:2019-01-01 Published:1905-07-14

摘要: 介绍了中国首次利用该技术成功开发高度衰竭后期的薄储高孔低渗的阿曼D油田碳酸盐岩油藏的实例。应用数值模拟方法确定了长水平段、小井距、跟趾反向部署、顶采底注的水平井整体注水开发的策略。首先开展先导试验,在成功实验的基础上,以精细的地质模型为基础,以水平井地质导向钻井技术为保障,推广完善了水平井整体注采开发井网。在水平井注采优化过程中,应用丰富的动静态资料了解注水动态,以流线模拟技术跟踪水驱油动态,从而调整注入和产出量,达到水驱均衡推进的目的。实践结果表明,水平井注采开发效果显著,以B块为例,截至2011年底注水增油量为220×104t,含水上升稳定,预计最终采收率可达44%

Abstract: The overall horizontal well waterflooding development of carbonate reservoir is without precedent in Oman. This paper introduces a case of China’s first use of the such a technology to successfully develop the carbonate reservoir with highly depleted, thin?thickness,high pore and low permeability in Oman?D oilfield. The reservoir and fluid characteristic indicates that this oilfield is suitable for horizontalwell waterflooding development, and the overall strategy of long?horizontal section, small well spacing, toe?to?heel reversed deployment and top?production and bottom?injection was determined by reservoir numerical simulation. Pilot test was first implemented. After the successful practice, based on fine geological model and guaranteed by geosteering horizontal drilling technology, the overall horizontal well injection?production pattern was extended and perfected. In the process of horizontal well injection?production optimization, the water injectionperformance was monitored by abundant dynamic and static data, and the displacement of oil by water was tracked by streamline simulation, then the injection and production volumes were modified to reach the goal of evenly displacing oil by injected water. The case study indicates that effect of horizontal well waterflooding development is remarkable. Taking Block?B as an example, its incremental oil was 220×104 t as of end of 2011, and water cut increased stably. The predicted ultimate recovery would be 44%

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