新疆石油地质 ›› 2003, Vol. 24 ›› Issue (2): 141-143+187.

• 油藏工程 • 上一篇    下一篇

调驱技术是低渗透油藏稳油控水的重要手段

李兴训, 张胜, 尹东迎, 冯业庆, 巴拉提·库尔班, 徐树森   

  1. 中国石油 新疆油田分公司 彩南作业区,新疆 阜康 831511
  • 收稿日期:2002-08-30 出版日期:2003-04-01 发布日期:2020-09-17
  • 作者简介:李兴训(1953-),男,甘肃民勤人,高级工程师,油藏工程。联系电话:0994-3840956

Profile Control and Displacement Method as an Important Means for Stable Oil Production by Water-Cut Control in Low Permeability Reservoir

LI Xing-xun, ZHANG Sheng, YIN Dong-ying, FENG Ye-qing, BARATI·Kurban, XU Shu-sen   

  • Received:2002-08-30 Online:2003-04-01 Published:2020-09-17
  • About author:LI Xing-xun (1953-), Male, Senior Engineer, Reservoir Engineering, Cainan Production District, PetroChina Xinjiang Oil, Fukang, Xin-jiang 831511, China.

摘要: 彩南西山窑组油藏微裂缝发育、储集层非均质性强,是典型的低一特低渗透油气藏。经过几年高速开发之后,因水窜、水淹而使油藏含水上升快、产量递减大、地层压力场分布复杂。对此,在深入进行油藏研究,认清砂层在纵向、横向上的发育程度、注采连通程度、储集层沉积微相、岩石物理相、储集层裂缝相、流体流动单元等油藏特征的基础上,对注水井进行普通调剖、深度调剖、“2+3”调驱等措施,使油层动用程度由68%提高至95% ,并且在横向上起到了深部液流转向的作用,较大幅度地提高了水驱波及体积和洗油效率,对整个油藏的稳油控水起了重要作用,而且投入产出比在1:3.5以上,经济效益显著。

关键词: 准噶尔盆地, 彩南油田, 低渗透油气藏, 波及系数, 驱油效率, 吸水剖面

Abstract: Xishanyao reservoir in Cainan oilfield is a typical low-extra low permeability oil pool with well developed micro-fracture and serious heterogeneity of reservoir. Following the several-year high level of production, it has appeared in quickly rising water cut, high pro-duction decline and complicated distribution of formation pressure field due to water breakthrough and watered out. Hence, a series of measures have been taken such as conventional and depth profile controls in water injection wells and "econdary plus tertiary recovery technologies”, based on in-depth reservoir studies in order to make sure development of pay zone in vertical and horizontal directions, connection between injection and production wells, reservoir depositional microfacies, petrophysical facies, fractural facies and fluid flow behavior. The results have shown that producing level of pay zone increases from 68% to 95%, enabling deep flow to be displaced transversely, and improving water flooding swept volume and displacement efficiency. Each injection well is stimulated, and followed by two production wells being responsible in average. W ater cut in the stimulated well group decreases from 4.5% to 2.9%, with production decline slowing down from 20% to 10%, along with input-output ratio over 1: 3.5. These profile control measures have played important roles in stable oil production by water-cut control for the whole reservoir, and offered significant economic efficiency.

Key words: Junggar basin, Cainan oilfield, low permeability reservoir, sweet fficiency, oil displacement fficiency, injection profile

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