›› 2015, Vol. 36 ›› Issue (3): 1-1.doi: 10.7657/XJPG20150312

   

Optimization of Long Core CO2 Huff and Puff Experimental Parameters in Low Permeability Reservoir, Yanchang Oilfield

HUANG Xiaoliang1, JIA Xinfeng2, ZHOU Xiang2, ZHENG Shanping3, YAN Wende1, YUAN Yingzhong1   

  1. (1.College of Oil and Gas Engineering, Chongqing University of Science and Technology, Chongqing 401331, China; 2. Department of Engineering, Regina University, Regina S4S0A2, Canada; 3. No.1 Production Plant, Xinjiang Oilfield Company, PetroChina, Karamay, Xinjiang 834000, China)
  • Online:2019-01-01 Published:1905-07-13

Abstract: By experiment of long core samples from low permeability reservoir in Yanchang oilfield, the effects of cyclic injection volume,soak time, pressure decline rate, gas injection process and gas injection rate on low?permeability reservoir development by CO2huff?n?puff process were studied. The results show that the first cyclic CO2 huff?n?puff is the key of production, its soak time should keep stable pressure followed by opening well for production, after which the production can be conducted without keeping stable pressure at any cycle.And appropriate low gas?injection rate may well overcome the influence of the model heterogeneity, hence reducing the negative impact of gas fingering on reservoir exploitation

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