新疆石油地质 ›› 2011, Vol. 32 ›› Issue (6): 675-677.

• 油气工程地质 • 上一篇    下一篇

不同黏度钻井液脱气效率实验

杨明清   

  1. 中国石化石油工程技术研究院,北京 100101
  • 收稿日期:2011-04-18 出版日期:2011-12-01 发布日期:2020-08-20
  • 作者简介:杨明清(1972-),男,黑龙江双城人,高级工程师,钻井工程,(Tel)010-84988380(E-mail)yangmq@sripe.cn.

Experiment of Degassing Efficiency for Different Viscosity Drilling Fluids

YANG Ming-qing   

  1. Research Institute of Petroleum Engineering, Sinopec, Beijing 100101
  • Received:2011-04-18 Online:2011-12-01 Published:2020-08-20

摘要: 准确检测钻井液内烃类气体含量是发现和评价油气显示的重要方式之一,然而钻井液黏度对检测结果存在很大影响。借助钻井液高温高压旋转模拟装置,进行了不同黏度钻井液的脱气实验,回归了不同黏度钻井液脱气效率图版及方程,建立了不同黏度钻井液校正系数图版及方程,可对现场测取的钻井液内烃类气体体积分数进行实时校正,有利于油气显示的及时发现和准确评价。

关键词: 钻井液, 黏度, 脱气效率, 影响, 校正系数

Abstract: Accurate detection of gaseous hydrocarbon content of drilling fluid is one of means for discovering and evaluating the shows of oil and gas. However, the viscosity of drilling fluid greatly affects the detection result. With the help of high-temperature and highpressure rotary simulator for drilling fluid, the degassing experiments of different viscosity drilling fluid are conducted, regressing the degassing efficiency chart and equations of the different viscosity drilling fluid, including establishing the coefficient-corrected chart and equations. By them, the real-time calibration of the volume fraction of the gaseous hydrocarbon in drilling fluid can be made at the well site, being good for timely discovery and exact evaluation of the shows of oil and gas.

Key words: drilling fluid, viscosity, degassing efficiency, affection, coefficient correction

中图分类号: