›› 2019, Vol. 40 ›› Issue (4): 1-1.doi: 10.7657/XJPG20190414

• 论文 •    

过热蒸汽改善驱油效果实验及机理分析

郭彬,林日亿,王泽宇,马强,王新伟   

  1. (中国石油大学(华东) 储运与建筑工程学院,山东 青岛 266580
  • 出版日期:2019-08-01 发布日期:1905-07-18

Experimental Study and Mechanism Analysis on Improvement of Oil Displacement Efficiency by Superheated Steam Injection

GUO Bin, LIN Riyi, WANG Zeyu, MA Qiang, WANG Xinwei   

  1. (College of Pipeline and Civil Engineering, China University of Petroleum, Qingdao, Shandong 266580, China)
  • Online:2019-08-01 Published:1905-07-18

摘要: 为探究注过热蒸汽对驱油效果的改善情况,通过室内单管驱替实验,研究蒸汽质量、注汽速率对采收率的影响,并从黏度、渗透率、热膨胀系数和蒸馏率4个方面对驱油机理进行分析。结果表明,当注汽速率为1.8 mL/min时,最优注入蒸汽质量为注过热15 ℃蒸汽,最终采收率可达77.8%;按照最优注入蒸汽质量注汽,最优注汽速率为1.3 mL/min,最终采收率可达79.6%;过热蒸汽驱替后,50 ℃原油黏度减小40.7%;实验用油平均热膨胀系数为0.000 653 ℃-1,原油温度增加300 ℃,体积增加19.6%;过热蒸汽促使蒙脱石和高岭石向绿泥石或伊利石发生转化,物理冲刷会使孔隙通道增大,改善储集层渗流状况。

Abstract: In order to study the improvement of oil displacement efficiency by superheated steam injection, an indoor single-tube experiment was carried out to study how the steam quality and injection rate influence the recovery factor, and the oil displacement mechanism was analyzed from four aspects:viscosity, permeability, thermal expansion coefficient and distillation ratio. The results show that when the steam injection rate is 1.8 mL/min, the steam with 15 ℃ degree of superheat is the optimal injected steam quality and the ultimate recovery factor can reach 77.8%; when the optimal steam quality is injected, the optimal steam injection rate will be 1.3 mL/min, and the ultimate recovery factor can reach 79.6%. After the oil displacement by superheated steam, the viscosity of heavy oil at 50 ℃ can be reduced by 40.7%. The average thermal expansion coefficient of the experimental oil is 0.000 653 ℃-1, the oil temperature increases by 300 ℃ and its volume will increase by 19.6%. The superheated steam will cause the transformation of montmorillonite and kaolinite to chlorite or illite, physical washing can increase the pore channel and improve the reservoir seepage behavior

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